| Improving Turnaround in Back Office Processes: A Lean-Six Sigma case study |
By Niraj Goyal
Background
Customer Delight (synonymous with Quality,
referred to in this paper as the big Q)
has 4 components: product quality, on-time delivery, service and
cost.
This case study demonstrates 3 significant aspects of Change
Efforts:
1 Improving three components of Q - product quality, delivery and/or service - inevitably leads to improvement of the fourth - cost – often much more effectively than pure cost reduction
initiatives. This principle is embodied in the COQ concept.
2 The Lean-Six
Sigma combine is much more powerful than either technique
individually. Real life problems typically consist of problems
in all three components of Q simultaneously.
Six-Sigma attacks defectives frontally while Lean attacks the
problems of cycle times, on time delivery and faster service
responses.
3 Time is a very effective overarching metric for measuring
and directing change in all the dimensions of Q.
It helps answer the often asked question – “Where do I start? Which
technique should be applied first?” It relentlessly forces the
blurring of artificial boundaries into seamless supply chains.
This
case was carried out in the high speed printing operation of a large
diversified, multi-location technical services provider in India.
The plant, engaged in outsourced printing work for a variety of
clients, struggled to achieve the turnarounds demanded. The project
was the pilot “demonstration” project for Lean-Six Sigma and
achieving the mindset change of operating personnel was as important
as the result’s achievement for the company to commit more resources
to the Q initiative.
The Case:
The narrative follows the chronological sequence of the seven steps of
problem solving.
Step 1 1.1) Selecting the Theme (CTQ) – Following a 2-day introductory “Quality Mindset Programme”
for senior management a brainstorm produced a long list of pain
areas for the organisation. These were separated into two
categories:
-
“End result” problems faced by external customers
-
Problems that were internal and therefore the causes of
customer problems rather than intrinsic problems in themselves.
A quick discussion led
to the realization that end result problems were the “real” problems (CTQs).
Using the weighted average table followed by a quick
discussion established the CTQ attribute - “Consistency in
Quality”.
1.2) Selecting the project - The management team then selected a location, a customer (Bank A),
and the team for a pilot project. The job involved the printing,
packing and despatching monthly bank statements for Bank A’s
clients. The work was therefore sporadic (once per month) with
unpredictable volumes.
A “Quality Mindset Programme” for the team was preceded the
project’s commencement.
Step 2 Defining the Problem: a group brainstorm regarding problems in customer line A was
prioritised. “Delayed turnaround” emerged as the critical
customer problem. The problem was defined numerically as
Problem = Customer Desire
– Current Status
Considerable debate was
required for all to agree the start and end points of turnaround as
“Arrival time of data on site” and “End of packing of all statements
for despatch”
Customer desire was ascertained from the Service Level Agreement (SLA) to be
specified at two stages of the process:
Printing turnaround 8133 images per hour
Job turnaround 8133 images per hour
TAKT time 0.43
seconds (3600/8133 seconds)
For determining the current state one run was followed through for
careful recording of throughputs and completion.
The TAKT time obtained was 1.35 seconds for a run of 56000
statements.
Problem: reduce TAKT time from 1.35 seconds to
<.43 seconds i.e. 67%.
Phase 1 Objective: reduce TAKT time 50%
Step 3
Finding Root Causes: Construction of the “Current State Value Stream Map” (A powerful Lean tool) was undertaken to unearth
problem areas for root cause and countermeasure analysis. This was
done in 3 stages
i) Outline process stages
ii) Agree “Best estimate” standard
times/cycle times expected for each activity
iii) Conduct a time study to ascertain actual
times.
Essentially the process has three major “loops”:
i) Pre-processing:
processing customer data, printing samples and getting customer
approval. This takes a fixed time independent of the volume and is
customer dependent.
ii) Printing and Slitting – high speed automatic machines
iii) Stuffing – labour intensive manual process with several stages
Based
upon data collected the Current State Value Stream Map shown in Appendix 1 was constructed. The Root
Cause/Countermeasure analysis for each loop proceeded as follows:
Loop 1 – Pre-processing
Step 3 Find the root causes In run 1 Pre-processing took
390 minutes as shown below:

Step 4 Generate Countermeasure Ideas:
With each activity timed, three successive brainstorms resulted in an idea to reduce this time from 390 minutes
<30 minutes. Essentially it meant
asking the customer to transfer sample data in “Flow” mode
before the main body of data arrived to enable approval to be before
the turnaround clock started.
Step 5 Check effects: In the third run 30 minutes
was achieved. Time had helped create a seamless
customer-vendor chain.
Step 6 Standardise the Process: this is in progess with the customer.
Printing and Slitting
Step
3 Find the Root Causes: The problem solving went through the following
cycle time (C/T) analysis using the classic Six Sigma cycle of
improvement:
- Establishing ideal C/T achievable.
- Determine actual C/T through time study, and
reason for all stoppages.
- Define the problem – (Ideal – actual) C/T
- Brainstorm root causes and countermeasures
- Implement countermeasures
- Check the results
- Repeat cycle
The
pre project results are summarised in Table 1 below.
Table 1
| Printing |
Cycle Time - secs |
| No of machines |
5 |
| Per machine (100% efficiency) |
0.27 |
| Actual C/T / machine (secs) pre improvement |
0.88 |
| Actual C/T without pre-processing |
0.51 |
| No of machines required |
2 |
| |
|
| Slitting |
|
| No of machines |
3 |
| Cycle Time |
0.1 |
Four
cycles of Observation – data collection - root cause –
countermeasure analysis were completed and implemented. Table 2
shows the analysis and Figure 1 the steady dramatic (50%) reduction
of cycle time from .74 to .36 seconds.
Table 2


Figure 2
The
required C/T (.43) had been achieved from one machine. Besides 1
machine was doing the job of 2 machines.
Stuffing turnaround had five main components as shown below:
| 1 |
2 |
|
3 |
|
4 |
|
5 |
|
| Pre |
Start |
Gap |
Start |
Gap |
Start |
Stuffing |
Stuffing |
Stuffing |
| Process |
Print |
2 hours |
Slit |
1.5 hours |
Stuff |
|
|
|
Pre-processing (1) and start of printing (2) had been reduced to
almost zero minutes.
Batch Processing between stages:
stages of a process often leads to large turnaround times.
Pre
project Slitting started 2 hours after printing due to batching in
printing – printed material was passed onto slitting only on
completion of “enough” material, as Slitting was much faster than
Printing. Flow processing was introduced and it was agreed that half
a batch (15 minutes) would be passed on to start slitting.
Likewise material from Slitting was passed on to Stuffing on
completion of a half batch in 15 minutes as compared to 1.5 hours
before the project.
With
pre-processing reduced to zero this meant that stuffing would start
30 minutes after the arrival of data.
Check the result: this
result was achieved in successive runs as shown below in Table 3.

Table 3
Obtaining a stuffing C/T of .43 therefore became the central issue.
Stuffing was mapped through its six stages, which were run in batch
mode. 2-3 large batches each of 1000 images envelopes were completed
by manpower shifting between stages as the batch progressed. The C/T
was .93 seconds and the productivity was 125 envelopes per man-hour
against the desire of .43 seconds and 250 envelopes per man-hour.
Each
operation was timed for its cycle time. A balanced line operating in
Flow with batches of 50 was set up. The cycle times and the
configuration of the flow line is shown in Table 4.

Table 4
The
concepts were tested first on a limited one-hour trial and then a
full scale run with dramatic improvements as shown in Table 5 below.

Table 5
Two
teams of 9 operators obtained a C/T of .3 seconds with a
productivity increase from 125 to 323 units per man-hour (i.e. 150%)
The
problem had been resolved and the new process was represented in the Future State Value Stream Map shown in Appendix 2.
Summary
of results: the
customer C/T .43 seconds was bettered to .36 seconds with a
productivity of assets and manpower increasing by 100-150% depending
upon the stages of the process as shown in Table 6.
| |
|
|
Manpower |
Machine |
| |
C/T |
C/T |
Productivity |
Productivity |
| |
Pre |
Post |
Increase |
Increase |
| Overall |
1.35 |
0.36 |
|
|
| Printing |
0.76 |
0.36 |
100% |
100% |
| Stuffing |
0.93 |
0.3 |
150% |
|
Table 6
Conclusion: The judicious mixture of lean-six sigma techniques produced a much greater improvement than any one
technique would have yielded. The Time metric
clearly pointed the way to which approach’s tools were most
appropriate at what stage of the project. Cost
reduction though not targeted resulted automatically with the improvement of Q.
Finally the company decided to continue the Q initiative.
Appendix 1 - Current
State Value Stream map

Appendix
2 – Future State Map


About the Author: Niraj Goyal has 25 years of experience with multinational companies in various
operating roles, among them operations director of Cadbury India
Ltd., where he was among the leading implementers of the quality
movement. He is the founder of Cynergy Creators Private Ltd. Mr.
Goyal consults in India, the United States and Southeast Asia with
manufacturing, IT, media and financial services industries. He
specializes in training and facilitating the implementation of the
techniques of Six Sigma-Lean and TQM. Several other real life case
studies can be accessed on his website www.nirajgoyal,cjb.net
Mr. Goyal can be reached at nirajgoyal@vsnl.in.
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